Jack Barlow
New member
1994 Johnson 225 J225TXERK
1,000 hours, excellent tough motor on a 1988 Grady White 24' Offshore purchased new in 1988. Old friends.
Engine is getting old and worn out, just like me. Would enjoy a few more hours of running up and down the Intracoastal here in Sebastian, Florida with my wife. Compression tells it all...70,70,60 -- 77,85,75. Have used OMC oil and "Carbon Guard" religiously with each and every tank of gas since new. Installed new head gaskets in 2010, cylinders all looked good, no scoring. "Deck" had the usual salt water use pitting. I carefully fixed that with JB Weld.
Engine was getting tricky to start. But ran strong up to the full 6,000 rpm @ 38 mph. If I recall correctly, I could do the low 40 mph when newer.
Finally would no longer start. Single cylinder spark tester showed no spark. Finally installed a used ebay stator, and had an immediate wonderful spark! My old stator had the usual melting down. Best spark in years... snap, snap, snap. You could easily hear it with engine running! I thought life was good again, but had idle issues. Not enough fuel pressure and would die after idling around. Started working on that issue by hooking up a separate tank to draw from. Ran that small container out of gas while testing. Would not start. Thought I had an air lock, took a line off after the filters. Gas flow was fine. Took a test and to my amazement, I had lost the spark again!!!
I'm totally lost. Even tried a known working power pack I had. No spark, either bank. Have the shift interrupter disconnected. Seemed to make the idle worse before the problems.
Tried disconnecting the big red plug. But could not get a screwdriver between the starter selenoid to spin the motor??? I used to jump the motor that way all the time, across the small two terminals? Batteries are good and spin the motor at 700 rpm indicated at tach. Nothing.
Pull the flywheel again? I have a used untested ebay timer base and a used, untested regulator. All the wiring around the power pack looks ok. Checked for pushed back pins. Removed black with yellow stripe wire on key switch.
Thanks fellows...
1,000 hours, excellent tough motor on a 1988 Grady White 24' Offshore purchased new in 1988. Old friends.
Engine is getting old and worn out, just like me. Would enjoy a few more hours of running up and down the Intracoastal here in Sebastian, Florida with my wife. Compression tells it all...70,70,60 -- 77,85,75. Have used OMC oil and "Carbon Guard" religiously with each and every tank of gas since new. Installed new head gaskets in 2010, cylinders all looked good, no scoring. "Deck" had the usual salt water use pitting. I carefully fixed that with JB Weld.
Engine was getting tricky to start. But ran strong up to the full 6,000 rpm @ 38 mph. If I recall correctly, I could do the low 40 mph when newer.
Finally would no longer start. Single cylinder spark tester showed no spark. Finally installed a used ebay stator, and had an immediate wonderful spark! My old stator had the usual melting down. Best spark in years... snap, snap, snap. You could easily hear it with engine running! I thought life was good again, but had idle issues. Not enough fuel pressure and would die after idling around. Started working on that issue by hooking up a separate tank to draw from. Ran that small container out of gas while testing. Would not start. Thought I had an air lock, took a line off after the filters. Gas flow was fine. Took a test and to my amazement, I had lost the spark again!!!
I'm totally lost. Even tried a known working power pack I had. No spark, either bank. Have the shift interrupter disconnected. Seemed to make the idle worse before the problems.
Tried disconnecting the big red plug. But could not get a screwdriver between the starter selenoid to spin the motor??? I used to jump the motor that way all the time, across the small two terminals? Batteries are good and spin the motor at 700 rpm indicated at tach. Nothing.
Pull the flywheel again? I have a used untested ebay timer base and a used, untested regulator. All the wiring around the power pack looks ok. Checked for pushed back pins. Removed black with yellow stripe wire on key switch.
Thanks fellows...

