Worth saying, motor runs, shifts cleanly, however water flow seemed a little weak hence looking to service/ replace the impeller. I did however notice a lot of what appeared to be salt deposits coming out of the inlets as I was manouvering the unit so this could have been part of the issue...
Hi, yes disconnected the shift shaft (after a bit of a fight). So far I have had zero movement which is what led me to believe there may be threads in the lower unit and the sheared bolt holding it. Now confirmed that's not the case, seems its a case of heat and patience.
Thanks for the reply :) That's what I hoped. The trim tab bolt sheered as well however, managed to drill that out. Looking at the bolt the threads seem to run into the lower unit, do they not? Thx
Hey all, hoping for some advice.
I was gifted a Concorde Chevalier by a friend.
Removing the lower unit from the yamaha 30hp and one of the four side bolts sheared leaving threads in top and bottom.
Initial thought was left hand drills and easy outs however, I don't seem to be able to get in...