trynhooker
Regular Contributor
This motor has no spark.
Mercury book tests dcv at black/yellow wires on both switch boxes with wires connected.
Should have 100-240vdc @ 400 rpm etc. I have 0 vdc.
So then book says disconnect black/yellow from both switch boxes and retest.
(1) If now normal, it is a wiring, ignition switch, kill switch issue. I removed kill switch, still 0.
(2) If still bad, test stator. Stator resistance all normal. Trigger resistance all normal.
Have to try disconnecting wiring harness to remove key switch after the flood goes away and also disconnect 2 yellow wires to reg and retest.
In the mean time, I'll continue.
INNER: With kill wires connected, stator output on blue wire <20vdc (should be 100-240vdc).
With kill wires disconnected, >200 vdc blue and kill wire connection.
OUTER: With kill wires connected, stator output on blue/white wire <20vdc (should be 100-240vdc).
With kill wires disconnected, < 20 vdc blue and kill wire connection.
So the above test points to stator. But....
Book also mentions about moving wires from one component to another to see if problem follow. If it follows its the stator, if it doesn't follow, it's the switch box.
So took blue and red from inner box and swapped with blue/white and red/white on outer box.
Problem stayed on inner box. As in, I still get the 20vdc on the "now" blue/white on inner box with kill wire connected, but good when kill wire disconnected. And same on outer.
Anyone one with more years of experience than I wanna jump on this one? I'm only in 10 years in the business since graduating school.
Let me also add, I disconnected the shift switch and the timing advance modules also. And even with the above testing, I've still not had any spark on either of the 6 coils. Had key switch in run position and using my remote start switch while testing to ensure spark would happen if things were working.
I'm so far stuck on IT'S THE SWITCHBOX and NOT THE STATOR since the problem stayed on outer switch box...as in the blue wire voltage didn't go up when it's kill wire was disconnected like the inner box did.
Mercury book tests dcv at black/yellow wires on both switch boxes with wires connected.
Should have 100-240vdc @ 400 rpm etc. I have 0 vdc.
So then book says disconnect black/yellow from both switch boxes and retest.
(1) If now normal, it is a wiring, ignition switch, kill switch issue. I removed kill switch, still 0.
(2) If still bad, test stator. Stator resistance all normal. Trigger resistance all normal.
Have to try disconnecting wiring harness to remove key switch after the flood goes away and also disconnect 2 yellow wires to reg and retest.
In the mean time, I'll continue.
INNER: With kill wires connected, stator output on blue wire <20vdc (should be 100-240vdc).
With kill wires disconnected, >200 vdc blue and kill wire connection.
OUTER: With kill wires connected, stator output on blue/white wire <20vdc (should be 100-240vdc).
With kill wires disconnected, < 20 vdc blue and kill wire connection.
So the above test points to stator. But....
Book also mentions about moving wires from one component to another to see if problem follow. If it follows its the stator, if it doesn't follow, it's the switch box.
So took blue and red from inner box and swapped with blue/white and red/white on outer box.
Problem stayed on inner box. As in, I still get the 20vdc on the "now" blue/white on inner box with kill wire connected, but good when kill wire disconnected. And same on outer.
Anyone one with more years of experience than I wanna jump on this one? I'm only in 10 years in the business since graduating school.
Let me also add, I disconnected the shift switch and the timing advance modules also. And even with the above testing, I've still not had any spark on either of the 6 coils. Had key switch in run position and using my remote start switch while testing to ensure spark would happen if things were working.
I'm so far stuck on IT'S THE SWITCHBOX and NOT THE STATOR since the problem stayed on outer switch box...as in the blue wire voltage didn't go up when it's kill wire was disconnected like the inner box did.