I have a 88 johnson 15hp long shaft outboard on my 14foot jon boat. It is a stubborn 2 stroke but works fine if you know how to deal with it. It is a long stroke that I had on too short of a transom, so Just before summer I replaced the transom on the boat and added a 5 in lift to get this motor to the correct height settings for the cavitation plate. Before I was having problems with the motor working too hard and inefficiently. On a couple longer rides last year it had started to smoke a little
Now that I have it back in the water at the proper height Ive noticed other problems. I took the boat to the water and was just checking the new transom for leaks and taking a couple laps to see how the motor was working with the lift. The motor was considerably faster and everything seemed be going swimmingly. I noticed a weak stream and was very happy with the strength and water tight transom so I took it out of the water pretty quick.
When I was backing into my drive way that day I thought with the lift I had added I did not need to raise the motor entirely but I was wrong. I scraped the fin and put a small bend in it.
So I replaced the impeller. The old one didn't look that bad but I replaced it anyway. I tried it on the water and there was a stream but still very weak. There was also a vibration in the motor that I attributed to the bend in the fin. After a while of having the boat out the stream stopped completely. I took it home and took it all apart again. I double checked everything was in the correct orientation again before putting it back together. I also took the bend out of the fin and sanded everything down smooth. I check the prop and it was fine.
I started it again on the muffs but still there was a trickle to no stream.
I ran some wire up in the peephole and sure enough sand came out. I punched some air through the peehole and a clog was released. I was ecstatic. I tried the motor again on the muffs and water came out in full stream. It started to give me 5 seconds of good flow then 1 second stop on a cycle. I think this was the thermostat letting the engine come to temp. Looked like everything was good to go.
I tried this morning to go fishing. The motor started quickly with good stream so I pushed off. The engine was vibrating pretty hard still but working and then 1 minute later the engine started pushing out white smoke from the pee hole with a weak/inconsistent stream. The smoke started coming out thick when I shut it down.
I let it sit for a few minutes at the dock and started it again. It cranked right over and looked fine for a few seconds then steam started coming off the peehole exhaust water. It escalated quickly and I shut it down again.
I was treating these symptoms as separate but now I'm thinking they are all connected. I have been learning everything as I go and have gotten by for a while but this is getting a little over my head. Any advice would be great!
Thanks
Now that I have it back in the water at the proper height Ive noticed other problems. I took the boat to the water and was just checking the new transom for leaks and taking a couple laps to see how the motor was working with the lift. The motor was considerably faster and everything seemed be going swimmingly. I noticed a weak stream and was very happy with the strength and water tight transom so I took it out of the water pretty quick.
When I was backing into my drive way that day I thought with the lift I had added I did not need to raise the motor entirely but I was wrong. I scraped the fin and put a small bend in it.
So I replaced the impeller. The old one didn't look that bad but I replaced it anyway. I tried it on the water and there was a stream but still very weak. There was also a vibration in the motor that I attributed to the bend in the fin. After a while of having the boat out the stream stopped completely. I took it home and took it all apart again. I double checked everything was in the correct orientation again before putting it back together. I also took the bend out of the fin and sanded everything down smooth. I check the prop and it was fine.
I started it again on the muffs but still there was a trickle to no stream.
I ran some wire up in the peephole and sure enough sand came out. I punched some air through the peehole and a clog was released. I was ecstatic. I tried the motor again on the muffs and water came out in full stream. It started to give me 5 seconds of good flow then 1 second stop on a cycle. I think this was the thermostat letting the engine come to temp. Looked like everything was good to go.
I tried this morning to go fishing. The motor started quickly with good stream so I pushed off. The engine was vibrating pretty hard still but working and then 1 minute later the engine started pushing out white smoke from the pee hole with a weak/inconsistent stream. The smoke started coming out thick when I shut it down.
I let it sit for a few minutes at the dock and started it again. It cranked right over and looked fine for a few seconds then steam started coming off the peehole exhaust water. It escalated quickly and I shut it down again.
I was treating these symptoms as separate but now I'm thinking they are all connected. I have been learning everything as I go and have gotten by for a while but this is getting a little over my head. Any advice would be great!
Thanks