76evinrude15
Member
Buddy and I took his boat out today after winter storage. Our day was wrecked because the motor would not run properly past 1/2 throttle. The motor runs fine at 1/2 throttle and below. When you try to go past that it sounds like the motor keeps shutting off cylinders. It would chug, then some cylinders would start to fire than they would stop firing again. No back firing.
When we pulled the pluggs out they were ALL soaking wet with gas. So I thought drying them would fix it. Nope, same thing. And if we pulled the pluggs they would be wet again. Tried 3 sets of plugs, all the same result.
Its a late 70's 50 horse merc thunderbolt.
Additional info. Last summer he bought the bought and from day one when you run the motor it ran fine, but when you stopped and fished for a bit when you try to turn the motor over it wouldn't start. You had to prime the bulb everytime you re started the motor. IF you didnt prime it until it was hard, it would not start. The motor was losing its prime after about 10 mins of sitting. We ran it like this all summer because we didnt want to be without a boat while repairing it and ordering parts.
This past winter my buddy took the fuel filter, fuel lines, and fuel pump off to see if he could find a leak. He didn't find a leak so he put it back together again. He didn't try it until today. And the motor held its prime all day. We didnt have to prime it once. So I am guessing the fuel filter, pump or fuel lines were loose and when my buddy put them back on he tightened some stuff up. In order to do this work he had to disconnect the choke and take off some wires. He said he put everything back on correctly using the repair manual. He also replaced the pluggs over the winter.
When he put the fuel pump back together he said he might have damaged the diaphram inside. He siad he didn't think he did, but when he was putting it together he might have.
And lastly, he had half a tank of reg gas left over from the fall. All he did was top the can up with fresh fuel today. No fuel stabilizer.
What I can think off
-old gas. We flushed the lines and tried fresh from the pump gas today. Did nothing. But maybe the old gas over the fuel gummed up his motor?
-Because my buddy might have fixed a vacum leak in the fuel system maybe he needs to re set the high speed jet? I can see the jet might be off because it was set to run with the motor having a vacum leak ...
-he DID damage the diaphragm.
-Something is amiss in the ingition. Coil? Timming? Points? Keep in mind it runs like silk at low speeds and idle and we tried 3 sets of pluggs.
Any help would be appriciated.
When we pulled the pluggs out they were ALL soaking wet with gas. So I thought drying them would fix it. Nope, same thing. And if we pulled the pluggs they would be wet again. Tried 3 sets of plugs, all the same result.
Its a late 70's 50 horse merc thunderbolt.
Additional info. Last summer he bought the bought and from day one when you run the motor it ran fine, but when you stopped and fished for a bit when you try to turn the motor over it wouldn't start. You had to prime the bulb everytime you re started the motor. IF you didnt prime it until it was hard, it would not start. The motor was losing its prime after about 10 mins of sitting. We ran it like this all summer because we didnt want to be without a boat while repairing it and ordering parts.
This past winter my buddy took the fuel filter, fuel lines, and fuel pump off to see if he could find a leak. He didn't find a leak so he put it back together again. He didn't try it until today. And the motor held its prime all day. We didnt have to prime it once. So I am guessing the fuel filter, pump or fuel lines were loose and when my buddy put them back on he tightened some stuff up. In order to do this work he had to disconnect the choke and take off some wires. He said he put everything back on correctly using the repair manual. He also replaced the pluggs over the winter.
When he put the fuel pump back together he said he might have damaged the diaphram inside. He siad he didn't think he did, but when he was putting it together he might have.
And lastly, he had half a tank of reg gas left over from the fall. All he did was top the can up with fresh fuel today. No fuel stabilizer.
What I can think off
-old gas. We flushed the lines and tried fresh from the pump gas today. Did nothing. But maybe the old gas over the fuel gummed up his motor?
-Because my buddy might have fixed a vacum leak in the fuel system maybe he needs to re set the high speed jet? I can see the jet might be off because it was set to run with the motor having a vacum leak ...
-he DID damage the diaphragm.
-Something is amiss in the ingition. Coil? Timming? Points? Keep in mind it runs like silk at low speeds and idle and we tried 3 sets of pluggs.
Any help would be appriciated.