"Weekend update...
Turns ou
"Weekend update...
Turns out the rockers are torqued to 22ft lbs. The crap Seloc manual and the 1994 merc manual did talk about doing the no lash/360 more thing. I found a 1999 merc manual #25 online at alt.mercury that set me straight.
On the Seloc manual... you guys were right. I can understand maybe having some details omitted, but to have info that is completely WRONG? Garbage.
Anyway, after setting the rockers to 22lbs it still performed badly.
Went to my machinist to pick his brain a bit on my issues and he pointed to either the carb or the ignition sensor in the distributor. So jumped into the carb. Took it apart and found that the float bowl was clean as a wistle. He theorized it may be gunked up with bad gas. Cleaned all the parts anyway and put it all back together. No luck. Still sputters at about 1800 rpm.
Stressing over the possibility that I did something really stupid like putting a piston in backwards, etc I started digging back into things.
Took the heads off and found that in my #6 cylinder there was foamed up oil (white stuff that happens when water and oil mix) on the head.
I was this far into it and had a weekend before I could order anything anyway, decided to keep going. Pulled the engine out of the boat, again.
Everything looked ok inside but while I was here thought I'd check the main and rod bearings.
Mains were in great shape. Pistons 6 and 4's bearings were badly scored. #4 had a groove in the middle of the bearing, and #6 had major scuff marks on the top and the bottom.
Replaced those bearings and started putting everything back together. Theorized the white gunk oil in #6 was caused by a bad seal on the head gasket, so this time I was triple sure all surfaces and gaskets were clean. Also, this time I was extra generous on the thread sealant on the head bolts too.
This morning I put the engine back in the boat, re-aligned it and slapped on the lower unit (went on so much easier this time, guess practice pays off eh?)
Fired it off and this time it immediately was able to go over 1800rpm, 2000, 2500.. anything, no problem!
After 15 minutes of running on the water hose I was convinced it was time to go for a test drive.
It ran great! I didn't go over about 3200 rpm as this was 'break in' time.
After about an hour of tooling around I did start to hear a rapping sound. I identified the area to be in the rocker arm covers. I figured one of the rockers had loosened so I took off the cover (brought ALL my tools with me)
Found the #6 intake rocker to be loose. Upon second glance I discovered WHY it was loose. The pushrod had 'pushed' clean through the rocker arm.
Ok,so why did this happen? I replaced lifters and pushrods, but did not replace rockers. Guess I should have?
I was able to putter back to the dock (2 miles) keeping it under 1800rpm.
Going to get the price on rocker arms tomorrow. If not too much I'm replacing them all.
Overall, I was pleased with the performance. I give it a B+ with a U in conduct though."